This is what I’ve been staring at the past couple of days. CAN bus issues. All the red X’s are no bueno.
Page 2 of the CAN bus issues. I enlisted the help of G3Xpert (Steve) via email and he quickly noted that my CAN bus terminator was missing the pins 3,4 jumper.
I incorrectly assumed that because this was specifically for terminating the roll/pitch servo connection the pins 3,4 would be terminated inside the connector. Don’t assume anything. The above pic is missing pins 3,4 jumpered together. Added the jumper et voila.
Now everything is working correctly. Thank you Steve! The AHRS issue you see above is because the OAT probe is not connected.